Part 7: A second chance… (maybe)
Luckily, since I was still at the beginning of the process, my blanks could be made reversible. This gave me a second chance at getting four identical cavities.
As mentioned earlier, nothing is simple. Because the bar of HSS was 4 1/4” long and I didn’t cut it shorter, it was engaged very deep in my collet. Since the same thing happened again, I got the answer about why I had different levels on my previous cavity. The tool was slowly pulling out of the collet as it was cutting so by the time the second side was cut the difference was several thousands of an inch.
Again I repositioned the cutter at the min and max levels to make both sides of the cavity identical.
Since I had three other cavities to machine, I placed a reference on the shaft of the cutter to be able to reset the starting depth position and it also confirmed that the tool was effectively creeping out when cutting.
I had to readjust the tool height several times (releasing and retightening the collet) and I guess there was some variations in the clamping because it was not pulling out consistently.
Again my hope of getting four identical cavities was out the window, instead I ended up with four variations of a similar shape.
The picture below shows the HSS cutter and a couple of views of the blocks.
Attachment:
H01.JPG [ 222 KiB | Viewed 370 times ]
Anyway at that point, I was glad enough to have something that was starting to look like a pellets mold. The job was not complete yet because it needed a pair of handles and a sprue plate.
I had a brand new “two cavities .380 round ball” Lee mold that I was keeping as a spare and I thought the handles would work well for my project. It seemed that they were attached with socket head cap screws but when I tried to loosen them with an Allan key I was unsuccessful. A quick Internet search confirmed that they can’t be removed. Luckily, I had a Noe .22 pellet mold with a set of handles that could be swapped.
For the sprue plate, I had to plan for a reversible arrangement to take advantage of the two sets of cavities.
Below there are several views of the finished mold.
Attachment:
H02.JPG [ 219.69 KiB | Viewed 370 times ]
Since I am not sure when I will be able to cast some lead with my finished mold, I used the hot glue gun to make several samples from each cavity.
A quick check showed me that both boo-boo cavities that were salvaged produced oversized projectiles. Because the material is plastic, the pellets could be pushed (or more precisely forced) into the barrel of the Gamo Compact and another break barrel pistol but in both they couldn’t be shot and jammed the airguns.
Lead will certainly be worse than plastic and will require a good look at existing resizing options. This might mean opening a Pandora’s box or a can of worms and even going down a rabbit hole.
I started with research on the Internet but I didn’t find what I needed. I made a tube from an aluminum rod by using sequentially larger drills to obtain some sort of taper that I smoothed off with sandpaper on a wooden shaft. The pusher was machined from steel with a tight tolerance with the exit hole. This time again it was a process of trials and errors.
Both of my first mistakes with the resizing tool were time consuming. I started by trying to resize a plastic bullet. It didn’t go well as it smeared the inside of the tube and the shaft of the pusher rod. I had to use alcohol to clean both parts. Then I thought I would try with lead because I have a full pot of spent pellets. I found a candidate and pounded it with a hammer to roughly make it cylindrical.
After placing the blob in the tube, the pusher rod was tapped with a hammer to progressively drive the lead down. I should have rotated and removed the rod periodically but instead I slowly tapped it from top to bottom until the “pellet” exited at the other end. For sure the blob got resized but it left a thin layer of lead shaving inside the tube effectively jamming the pusher rod. Let say it took a lot of time to back off the rod out and scrape the layer of lead flakes from inside the tube.
This picture shows my first attempt at making a resizer after it was cleaned up.
Attachment:
H03.JPG [ 91.57 KiB | Viewed 370 times ]
Another search, a bit too late, made me realize that lubrication was a must.
Anyway my journey in resizing is another story so it will be the subject of a different post.
In conclusion, D type single flute cutters are good options to shape pellet cavities in aluminum blocks but I would stick to High Speed Steel if I have to do it again. The drill rod stock might be useful for larger diameters but at the size I was working for that project it was too easy to break.
R-Gun Pete